I�ve finally managed to put together some pictures of my
Cold Smoker build, it�s been running for the last two days. I tweaked the design a little and have added details of these.
Traditional cold smoker designs allow fresh air to be freely drawn over the open fire and into the smoker such that the smoke emerging is thin and wispy - not dense. If insufficient fresh air then the smoke is too hot and, even with dry wood, too humid, 80 % relative humidity is ideal. This is because the process of burning gives off carbon dioxide and water vapour. A lower smoke temperature gives better smoke diffusion but needs longer smoking times. it is a slow process and hams can be smoked from 2 to even 6 weeks.
I was aiming for a medium scale DIY cold smoker that (as I want to do hams) would run as long as possible without attention and was cheap to produce � ideally using mostly materials to hand (junk). Having been given a large cask all I�ve had to buy is a 100 mm Flanged Spigot at �2.40.
My smoker consists of a combustion unit that generates dense smoke and a mixing unit that combines the smoke with a large amount of fresh air. The smoking chamber, a Whisky cask (Hogshead size) stands on three concrete blocks that make room for mounting the mixing unit on the underside of its base.
A 4 foot length of 10mm copper pipe carries the dense smoke from the combustion unit to the mixer. Due to the slow airflow and rate of burn the water vapour from the burning process tends to condense in the copper pipe. The pipe run was shaped (it bends easily by hand) with a definite bend at the lowest point. A condensate drain hole (3.2mm) was drilled in the bottom of the pipe at this low point.
A burner design where airflow relies on convection is sensitive to wind, local turbulence and air pressure variations, e.g. chimney downdraught. The smaller the fire the worse the problem, it tends to either go out or flare up and get too hot. We often get strong winds here so I�ve used fans to give the controlled airflow needed. Both are PC processor cooling fans, their small size being an ideal fit with the other smoker parts. I had a scrapped 486 PC and another scrap motherboard so that gave me two small 12 Volt fans and a supply of 12 Volts.
I�ve put the PC case in an outbuilding and ran the 12 Volt supply to the smoker using bell wire.
The combustion unit is basically a vertical tube through which air is blown, it is made in two parts- the blower and the combustion chamber. This makes it easier to remove the combustion chamber to empty it.
The combustion chamber is two large tin cans joined together end to end, each is 4� diameter by 8� long . The can ends are all removed except the bottom end this has three 3.2mm holes drilled for air to enter. Note that the size and number of these holes, together with the blower fan speed, controls the burn air flow (I started with two smaller holes for the test run and drilled extra as required).
To join the cans I wrapped a 2 inch strip of scrap lead flashing around the join and twisted some galvanised wire tightly round while tapping the lead to form it round the can rims.
The combustion chamber stands on the blower unit which I made from another slightly larger tin can (a cleaned out 1 litre paint tin). This has four 5mm holes near the centre (below the combustion chamber), and has a fan mounted on its side to blow in air. The can side was pushed in to flatten it a little and a 56mm diameter hole cut with tin snips. Four small self tapping screws, that came with the fan, fix the fan on.
I wanted to be able to control the fan speed. Some PC cooling fans have a speed control, this one didn�t so I wired a 200 ohm wire-wound potentiometer in series to do the job.
I needed a detachable lid for the top of the combustion chamber, I couldn�t find a close fitting tin (that would fit over) so had to fashion a lid from scrap metal. I used a 6inch circle cut from scrap lead flashing, this was tapped into a lid shape using the can base as a former.
I cut a 15mm diameter hole in the lead lid, and in one of the removed tin lids, to take the end of a 10mm copper pipe compression fitting to act as a pipe flange. The fitting sandwiches the two lids together, the tin lid going under the lead to act as a heat barrier and stiffener. The 10mm smoke pipe is just left loose in this fitting so it can be lifted on and off.
I used a length of 6 inch diameter clay field drain as an outer sleeve around the combustion unit (including the fan). This makes it more stable, also the incoming air is warmed as is drawn down between the outer sleeve and the combustion chamber. This (secondary) combustion method means that a slower fuel burning rate can maintain the combustion. For a small barrel smoker there�s more than enough smoke at the slowest burn rate possible.
SMOKE CHAMBERThis was an enjoyable task - in a small workshop the whisky fumes were quite overcoming.
The cask lid was first removed by cutting around it. Sixteen � inch holes were drilled in the lid and covered with perforated zinc. Across this are three batens at right angles that hold the lid planks together, and create an air gap; over these is an oversized rain cover. I used galvanised steel sheet for the cover, with the edges bent down to shed water, and screwed a wooden handle, cut from a short length of (2� x 1�), to the centre batten.
A 100mm diameter hole was cut in the cask base and over this stood a baffle on � inch spacers. The baffle spreads the incoming jet of smoke-air.
I�ve arranged supports that allow for hanging meat and using a grid shelf.
Two 10mm copper coated steel rods (an electrical earth rod cut in half) go through holes drilled near the top of the cask. The rods are parallel and across them rest notched wood battens, for hanging meat, and/or an old BBQ grid shelf. Meat is tied to a batten then lifted in or slid along the rods together.
The mixing unit adds a relatively large amount of air to the dense smoke. Air from the fan is formed into a jet by the nozzle and smoke from the combustion unit is added at this point. Where air speeds up to go through a constriction the air pressure drops (the Venturi effect) this helps draw smoke from the combustion unit � rather than try to blow it back.
I�ve fixed a 100 mm Flanged Duct Spigot to the bottom of the barrel where I�d cut a 100mm diameter hole. After cutting its top rim off, the tin can I used fitted exactly over the spigot. I�d bought this spigot for my mk1 smoker design (electric hob & gutted microwave), otherwise I�d probably have fitted the can direct cutting 3 inch holes in its base and in the barrel.
The fan is fixed, with self tapping screws, over a 45mm diameter hole in the bottom of the can. A piece of fine mesh to stop insects is sandwiched between the can and the fan.
I used part of a plastic juice bottle for the nozzle, one that was a reasonably tight fit over the fan. I drilled a 10mm hole in its neck for the smoke pipe and another level with this in the can wall. Where the pipe enters I used a 10mm copper pipe compression fitting (drilled out to let the pipe go right through) but just a tight hole in the can would have done.
MIXER AND BLOWER
LOOKING DOWN THROUGH THE CASK BASE HOLE
BurningTest run
Initial tests of the combustion unit alone used Pine shavings and chunks up to 2 cubic inch. Little combustion airflow was needed, otherwise there was a tendency for it to flare up if the lid was removed. A surprising amount of liquid tar ran down from under the lid.
With the mixing unit and smoke chamber connected tests using Plum wood chips and chunks revealed that there was insufficient air flow to maintain combustion. The number and size of the holes in the combustion chamber base was increased (to 3 x 3.2mm).
The smoke from the combustion unit is about 10� C when it reaches the far end of the copper pipe.
On the test day the (damp) air temperature was 8� C and in the barrel was 6� C. This must have been due to the cooling effect of evaporation from the whisky soaked wood. An inspection light was left to warm the barrel overnight with the fans running to dry it out.
The first smoking day it went out after around 2 hours, the fuel hadn�t settled so emptied and relit. Eventually the fuel ran out after between 8 and 9 hours, fans switched off at 9hr point. Second day, still burning at 9 hours when fans switched off.
I would expect that a full load of shavings only would last less than an hour, and a chippings only maybe 2 � 3 hours. I�m experimenting with the best wood size mix to use, currently using Plum wood:
To light � a handful of shavings, burning scrap of paper then two handfuls of shavings added a little at a time.
Getting going � a few handfuls of chippings (from cutting with chainsaw)
Fill to top � mix of wood chunks and more chippings, starting with small chunks and building up to about 1 cubic inch. Then put on lid and attach the smoke pipe.
I�ve run the burner fan at full speed for the first 2 hours or so, to get the combustion chamber hot, then reduced it slightly to give less smoke and a longer burn time. On the test day there was cold damp drizzle all the time, the fan had to be kept at maximum.
A full load will burn for over 8 hours but needs an occasional poke with a stick to settle the fuel, every hour or two or when the smoke is becoming thin, otherwise it can go out. As it burns a cavity must form under the fuel, if the burning fuel falls to the bottom then the heat wouldn�t reach the remaining fuel. The ribs in the can walls or the seams at the join may be the problem.
SmokingWe were using fresh back and streaky bacon, from our own pigs, that had been dry cured.
Day 1. Air temperature was 4.8� C and in the barrel was 3.9� C Not sure if this drop is due to further whisky evaporation or the back & streaky bacon drying off. Not ideal as relative humidity will be higher than outside. The bacon colour does not seemed to have changed yet, probably due to the low smoking temperature.
Day 2. Continued smoking bacon. To increase the temperature I�ve added a 21Watt car bulb, temporarily loose just under the baffle. Its fed off the PC 12V via another length of bell-wire. Now air temperature 7.5� C and in the barrel was 9.3� C
A test batch of Cheddar was also done � 1/5th not smoked, 1/5th smoked 1hour, 1/5th smoked 2 hours, 1/5th smoked 3 hours and 1/5th smoked 4 hours. Wrapped and will taste after 5 days.
The bacon has been smoked for around 17 hours. It smells very smoky but didn�t appear obviously darker, however comparing it against unsmoked bacon showed a light golden brown tint. We properly tested some streaky bacon at lunchtime. The colour and smell ran right through the slices and the result got 10/10 all round.
Modifications - perhapsIf the heating lamp continues to be needed (whisky finished evaporating ?) it will need to be mounted somehow. To get a bit nearer 12�C maybe I�ll need either increased bulb wattage or reduced fresh air flow (a second fan speed control).
The tin cans used for the combustion unit would be better replaced by a stainless steel tube, smooth so fuel might settle better and will last longer. I�ll be on the look out for off cuts of chimney section.
Having removed the cask lid it, and before the wood shrinks as it dries, I should strengthen the cask by screwing the metal bands onto the oak planks. Stainless steel screws are best, others will stain the oak.
PARTS LIST
Smoke chamber. . . . . . . . . . . . . . . . . . . . . whisky cask
Insect mesh. . . . . . . . . . . . . . . . . . . . . . . . perforated zinc, fine plastic mesh or microwave door mesh
Rain cover. . . . . . . . . . . . . . . . . . . . . . . . metal or plastic sheet or thin ply
Two support rods. . . . . . . . . . . . . . . . . . . . . copper coated steel earth rod1.2m x 10mm
Two small 12V fans. . . . . . . . . . . . . . . . . . . . . PC scrap
12 Volt power supply. . . . . . . . . . . . . . . . . . . . . PC scrap or 12V dc supply mains block.
DC fan speed control. . . . . . . . . . . . . . . . . . . . . 200 ohm wire-wound potentiometer (volume control)
Tins for blower unit and mixing unit.. . . . . . . . . . . . . . . 1litre paint tins
Tube for combustion unit, with base and removable lid. . . . . . . . . Two 8inch by 4inch diameter tins
10mm copper pipe, 4 foot length. . . . . . . . . . . . . . . Central heating pipe
Flange for 10mm pipe. . . . . . . . . . . . . . . . . . . . . 10mm compression fitting
Air jet nozzle. . . . . . . . . . . . . . . . . . . . . . . . Plastic juice bottle
Baffle plate 6inch diameter. . . . . . . . . . . . . . . . . . Copper sheet or thin plywood
100 mm Flanged Duct Spigot (optional)
The way out is through the door.